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Casing failure identification of long-abandoned geothermal wells in Field Dieng, Indonesia

Marbun B.T.H.a, Ridwan R.H.b, Sinaga S.Z.a, Pande B.a, Purbantanu B.A.a

a Petroleum Engineering Study Program, Bandung Institute of Technology, Bandung, 40132, Indonesia
b PT Geo Dipa Energi, Jakarta, Indonesia

[vc_row][vc_column][vc_row_inner][vc_column_inner][vc_separator css=”.vc_custom_1624529070653{padding-top: 30px !important;padding-bottom: 30px !important;}”][/vc_column_inner][/vc_row_inner][vc_row_inner layout=”boxed”][vc_column_inner width=”3/4″ css=”.vc_custom_1624695412187{border-right-width: 1px !important;border-right-color: #dddddd !important;border-right-style: solid !important;border-radius: 1px !important;}”][vc_empty_space][megatron_heading title=”Abstract” size=”size-sm” text_align=”text-left”][vc_column_text]© 2019, The Author(s).Integrity issues create challenges for maintaining the production of mature geothermal wells. Such problems are likely to occur in wells designed according to oil and gas standards, without considering the extreme geothermal environment. PT Geo Dipa Energi as the operator of the Dieng geothermal field, one of the longest operated in Indonesia, has experienced this difficulty since acquiring the field. Almost half of the production wells have been abandoned because of casing issues. To increase production, the operator plans to reactivate wells that have been previously abandoned. An initial study was performed to assess the technical feasibility of reactivating wells at Dieng; it included the development of a well assessment methodology including casing design, comprising historical data analysis, identification of well problems, and investigation of well integrity. The study focused on the identification and characterization of two abandoned wells, HCE9B and HCE28B, current casing conditions, limitations, and challenges to perform a well intervention and workover which is realistic, measurable, economic, and technically feasible. The result of this study will be applicable for casing design for future wells.[/vc_column_text][vc_empty_space][vc_separator css=”.vc_custom_1624528584150{padding-top: 25px !important;padding-bottom: 25px !important;}”][vc_empty_space][megatron_heading title=”Author keywords” size=”size-sm” text_align=”text-left”][vc_column_text]Assessment methodologies,Casing design,Casing failures,Historical data,Increase productions,Production wells,Well intervention,Wellbore[/vc_column_text][vc_empty_space][vc_separator css=”.vc_custom_1624528584150{padding-top: 25px !important;padding-bottom: 25px !important;}”][vc_empty_space][megatron_heading title=”Indexed keywords” size=”size-sm” text_align=”text-left”][vc_column_text]Casing design,Casing failure,Geothermal wellbore,Well integrity[/vc_column_text][vc_empty_space][vc_separator css=”.vc_custom_1624528584150{padding-top: 25px !important;padding-bottom: 25px !important;}”][vc_empty_space][megatron_heading title=”Funding details” size=”size-sm” text_align=”text-left”][vc_column_text][/vc_column_text][vc_empty_space][vc_separator css=”.vc_custom_1624528584150{padding-top: 25px !important;padding-bottom: 25px !important;}”][vc_empty_space][megatron_heading title=”DOI” size=”size-sm” text_align=”text-left”][vc_column_text]https://doi.org/10.1186/s40517-019-0146-3[/vc_column_text][/vc_column_inner][vc_column_inner width=”1/4″][vc_column_text]Widget Plumx[/vc_column_text][/vc_column_inner][/vc_row_inner][/vc_column][/vc_row][vc_row][vc_column][vc_separator css=”.vc_custom_1624528584150{padding-top: 25px !important;padding-bottom: 25px !important;}”][/vc_column][/vc_row]